Showing posts with label clutch. Show all posts
Showing posts with label clutch. Show all posts

Thursday, August 8, 2013

Mantling and Re-assembly: 1969 Karmann Ghia engine overhaul, part 3

Part of the fun of new experiences is that they can turn out quite differently from what you might have expected. When I posted Part 2 of this series, I thought I was going to take the cylinder heads and the crankcase from my Ghia to a local machine shop: The cylinder heads for a valve job, the crankcase to be examined for cylinder/piston wear. To make a short story shorter, that's not exactly what happened.

Remember I said that when I took off the clutch plate, I discovered the flywheel was loose? Well, it's not supposed to be loose, not even a little bit. The flywheel is attached to one end of the crankshaft, which is, you know, what makes your car go. What I found out was that, because the flywheel had been loose (and presumably getting steadily looser over time), the bearing that the crankshaft end goes through was no longer round. There was too much "play" because of the loose flywheel, beating up on the bearing to where it was, even to my untrained eye, slightly oval. At that point I wasn't surprised when the mechanic told me that the crankshaft itself, and the crankcase, were "probably toast". (I think he was trying to be diplomatic.)

So I asked him what my options were. The upshot was that he thought my best bet would be to shop for a good used engine. What would that cost? Well, he said, you could easily spend $1000 or more. He gave me a few tips on what to look for, and I sadly packed up my cylinder heads and went home.

Shopping was discouraging. The only used motors I could find that were a close enough match for my car were located out of state. Many were priced at over $2000. I put my own ad on Craigslist, saying I was looking for a motor for my Ghia.

The next day I was contacted my someone in Lake Stevens (not close but north of Seattle, not all that far away) who had a Volkswagen shop. He sold me a nice rebuilt longblock (the guts of the engine: crankcase, cylinders/pistons, heads and valves) for $400. The rest of the parts, distributor, carburetor, fan housing etc. from my old engine were still in good shape, so all I had to do was put it all back together.


New longblock with new crank pulley (center bottom) and oil cooler in place.

First I installed a new crank pulley. It's definitely an improvement on the old one, as this one has degree markings all the way around. When you adjust the valves or set the ignition timing, the engine is rotated half a turn at a time, so the marks make it easy to do this accurately. It is also made of aircraft-grade aluminum, which won't rust like the old steel one. This is better because a rusty pulley can eventually do bad things to your fan belt.

 Crank pulley showing timing marks.

Next I installed the generator, fuel pump, and generator stand. Then the heat exchangers. Piece by piece the engine shrouding went in. I had bought a new muffler as the old one had at least one noticeable rust hole. After the muffler came the intake manifold, with carburetor attached. Finally, the fan housing and generator slid into place over the oil cooler.

Re-assembled engine, just about ready to go back in!

Now all I need to do is install the fan belt (easier to do with the engine out of the car), double-check that spark plugs and all fasteners are tightened, hook up the new spark plug wires, and I'll be ready to put the engine back in the car. 

 The empty engine compartment.

 
New clutch throwout bearing in place; the doughnut-shaped thing in the middle.

The last thing I did was to replace the clutch throwout bearing (see photo above). I didn't even know (blush) that the clutch lived right at the junction of the engine and the transmission. Since I had the opportunity, I had replaced the clutch plate, which lives between the clutch pressure plate and the flywheel. 
Back of re-assembled engine: The round thing in the middle is the clutch pressure plate.

I've been pretty busy with other projects lately, like my first book, which is going to be published very soon now. So I have been taking my time with this project, sometimes not doing a thing on it while waiting for a new part to arrive. Still, I'm pleasantly surprised at how relatively quickly I took the thing apart and got it back together. In my next post, I'll list the time I spent, what I spent on parts, and hopefully, have some photos of my little car all put back together!



Thursday, June 27, 2013

Stripping and dismantling: 1969 Karmann Ghia engine overhaul, Part 2


Well, here it is: the engine is out of my Ghia. I am pleased to report that I was able to get this far on my own. (David did help me jack the car up, though.) The engine, with all the stuff still attached as shown here, weighs something over 200 pounds. First, I had a piano dolly blocked in place under the engine. Two scissors jacks on the dolly were then raised to where they were in contact with the oil pan, to support the engine once it came off the upper and lower mounting bolts, which hold the engine onto the transmission. With one hand on the fan housing (the curved black box at the top center of the photo) and the other on one of the tailpipes, I carefully wiggled the engine off the bolts until it was resting on the jacks. I then lowered the jacks so the engine could be rolled out from under the car.


Now the engine stripping begins! This photo shows the engine after I took off the fan belt, fan housing, intake manifold and carburetor. The tall black skyscraper-looking thing is the oil cooler. I had suspected the oil cooler was leaking, and sure enough, one of the two seals at its base was bad. Since the cooler lives inside the fan housing, when it leaks, the fan tends to fling oil all over the engine area, hence my suspicion.

After I took off the oil cooler, I removed the muffler (the rusty-looking thing at the bottom of this photo) and the two heat exchangers. The weight of the engine was now down to around 150 pounds, and I rolled it on its dolly into the shed so I could get it up onto the Workmate and be under cover as well. Between David and I we had no problems lifting it up onto the Workmate.
 

So here's the stripped-down engine, up at a good working height. What you're looking at in the middle of this photo is the clutch plate, which is attached to the flywheel. On either side are the cylinder heads with valve covers still in place. next job is to remove the clutch plate and the pressure plate under it, then the flywheel.


With the clutch removed, I used this nifty little flywheel lock to clamp the flywheel in place prior to removing the large gland nut that attaches the flywheel to the crankshaft. At this point I had a surprise: The 36mm gland nut, which is supposed to be torqued to 220 foot-pounds, was actually loose. I had expected to need a breaker bar and someone stronger and heavier than me to loosen the thing. Instead, after barely a quarter turn with the socket wrench, I was able to unscrew it the rest of the way by hand.

Aha, I thought. I bet the ka-thunk ka-thunk ka-thunk noise I was hearing (thinking this was a thrown connecting rod) was coming from this loose flywheel. The good news is I took the thing apart before the flywheel came all the way off. The bad news is that, because of the way the thing was wobbling around in there, I'll almost for sure have to replace the crankshaft. No doubt I'll have a list of things to take to the machine shop.


In the meantime, I next removed the rocker arm assemblies and cylinder heads. The rocker arm is the pipe thing going from left to right, with four little arms attached. Here I've removed the two nuts holding it in place. Then it is simple to lift the assembly up and out.


After the rocker arms are out, the eight nuts holding the cylinder head in place are easy to reach and loosen. Here you can see I've taken off one of the cylinder heads (on the bench to the right). Toward the top center of the photo, the round black things are two of the four cylinders, with pistons inside. The only thing left to do before opening up the crankcase is to remove the cylinders and pistons.

I was fortunate to discover a shop in Port Angeles (about half an hour away) that specializes in air-cooled Volkswagen repair. I will be taking the cylinder heads there to have the valves done (something I do not have the specialized equipment to do). They will also check the flywheel for possible damage, since it was loose, along with the crankshaft. After that, I will be able to start putting it all back together!

The thing that has surprised me the most about this project is that I have only spent about seven hours so far. Considering I had never done anything like this before, I'm kind of amazed that it has seemed so relatively easy. I've been taking my time, too.

I'll have another update after the machine shop does its work. I'm starting to think I'll be driving my Ghia again before long! What a fascinating project.